MindMap Gallery Process department consumption reduction project planning
The following is a summary of the consumption reduction project planning of the process department. The knowledge content includes acid consumption reduction, slurry consumption reduction, special gas reduction, energy consumption reduction, diffusion new process promotion, wire mesh knot-free promotion, etc.
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This is a mind map about bacteria, and its main contents include: overview, morphology, types, structure, reproduction, distribution, application, and expansion. The summary is comprehensive and meticulous, suitable as review materials.
This is a mind map about plant asexual reproduction, and its main contents include: concept, spore reproduction, vegetative reproduction, tissue culture, and buds. The summary is comprehensive and meticulous, suitable as review materials.
This is a mind map about the reproductive development of animals, and its main contents include: insects, frogs, birds, sexual reproduction, and asexual reproduction. The summary is comprehensive and meticulous, suitable as review materials.
Process department consumption reduction project planning
Reduced acid consumption
HF consumption reduced by 20%
Adjust the etching tank formula, and reduce the self-replenishment from 27.2L/10,000 pieces to 24L/10,000 pieces, a reduction ratio of 11.6%
Reduce the HF consumption of pickling after etching, and the self-replenishment is reduced from 8.4L/10,000 pieces to 4.0L/10,000 pieces, a reduction ratio of 52.3%
The HF consumption for cleaning after texturing was reduced from 8.8L/10,000 pieces to 7L/10,000 pieces, a reduction ratio of 25.7%. The formula was adjusted on 6/29.
The next step is to reduce it to 6.3L/10,000 pieces, a reduction of 10%.
The pickling and consumption reduction after etching has been completed before. In order to control the proportion of black spots and restore, it is expected to restart on Sunday. The total HF consumption reduction is expected to be about 20%. Since the production line is increasing production and opening up, in order to improve the cleaning effect, the newly opened line has not yet reduced consumption.
HNO3 consumption reduced
Adjust the etching tank recipe
It will be carried out after the etching HF reduction is completed. The specific reduction ratio needs to be evaluated. It is expected that the preliminary evaluation results will be released on July 9 and the entire line will be completed on July 13.
Reduce hydrogen peroxide consumption by 58%
With the introduction of Feilu pre-cleaning additives, the self-replenishment volume is expected to be reduced from 53L/10,000 pieces to 25L/10,000 pieces, a reduction of 53%. Sanfeng cleaning agent has been used in batches on 6/28 and has been reduced to 20L/10,000 pieces.
Topband cleaning agent has completed three lines. As the business and technology center prepares to introduce a second supplier, the line expansion plan is suspended. The consumption of imported lines has been reduced by 40%, and the current unit consumption is 33L/10,000 pieces.
Pure water consumption reduced by 25%
The overflow method of texturing was changed from constant overflow to basket overflow, and the overflow volume was adjusted at the same time. The unit consumption was reduced from 17 tons/10,000 pieces to 11 tons/10,000 pieces. Changes across the board this Friday
The overflow volume has been adjusted from 1000L/H to 600L/H, and has been reduced to about 13 tons/10,000 pieces. The overflow method was changed to basket overflow on July 7, with the final target of 11 tons/10,000 pieces.
Slurry consumption reduction
Back silver consumption reduced to 25.5mg
Yarn thickness reduced from 60 to 56
Film thickness reduced from 10 to 8
The sample test has passed, the test screen paste weight is 25mg, and the batch screen has been purchased.
Back aluminum consumption reduced to 240mg
Back field film thickness reduced from 20 to 16
Backfield line width reduced from 120 to 105
The sample test slurry weighs 200mg, and 5 medium batch screen plates have been purchased and will arrive on July 13 for batch use.
158 positive silver consumption reduced to 60mg
Knotless screen printing was introduced, and the simultaneous film thickness was reduced from 10 to 7
The high-quality batch, Minglu 63mg pulp weight (65mg actual unit consumption) screen version has signed ECN, the import was successful, and the wet weight screen version has been further reduced and is being purchased.
Reduced special energy
Reduce silane and ammonia consumption by 10%
Adjust the ratio of SiH4 and NH3 in the front and back films. The current theoretical consumption of silane is 0.73kg/10,000 pieces and ammonia is 3.10kg/10,000 pieces. After the reduction, the consumption is 0.66kg/10,000 pieces and 2.9kg/10,000 pieces, respectively, a reduction of 11%.
For machines whose RF power has not reached the maximum, adjust the RF power to the maximum to reduce ventilation time and special air consumption.
Batch switching has been completed. Recently, due to the production line opening, there are many saturated boats, resulting in high special gas consumption.
Reduce laughing gas consumption
Design gradient experiments to reduce N2O flow in the back film process of the ALD route
Develop a new back film process, adjust the film thickness and structure of silicon oxynitride and silicon oxide, and reduce N2O experiments in the CT two-in-one route
Try to develop new processes, cancel the SiNxOy and SiOx film layers of the ALD route, and stop using laughing gas
After comprehensive evaluation, the efficiency loss is unacceptable and will not be reduced.
Reduce the amount of nitrogen used in the process
Adjust the large nitrogen flow rate of the diffusion process to reduce the diffusion nitrogen consumption (the coating vacuum pump has been adjusted twice, and if the flow rate is reduced, the vacuum pump will frequently get stuck)
The graphite boat cleaning agent bubbling is changed to air pressure. Nitrogen usage was reduced to 5%.
The nitrogen consumption reduction target is 293kg/10,000 pieces.
Reduced energy consumption
Adjustment of screen air pressure flow to reduce screen air pressure by 50%
Adjust the pressure air flow of the sintering furnace and synchronize the sintering curve to ensure efficiency and yield, reduce pressure air consumption, and thereby reduce energy consumption.
Formulate adjustment rules for sintering furnaces, and adjust the pressure air within the specified range to prevent the adjustment of pressure air consumption.
Preliminary consumption reduction has been completed. The preliminary reduction in air consumption is about 50%. The tracking of sintering defects is stable, the efficiency is no abnormal, and the power consumption is reduced by 100 kWh/10,000 pieces.
Wire mesh without knots improves efficiency
Find a suitable screen manufacturer
Good product
famous road
Lebon
Hengsheng
Among the four screen manufacturers, taking into account lifespan, unit consumption and efficiency, Liangpin, Minglu and Lebang can be qualified suppliers. Lebang is an alternative supplier due to its higher price.
Match three screen film thicknesses
12 film thickness
11 film thickness
10 film thickness
8 film thickness
The film thickness is thicker. When it is 12 microns, the unit loss is high and the grid is seriously broken. The film thickness is reduced to 8. The wet weight is too low and the tension and reliability are not controlled. After comprehensive consideration, the film thickness is controlled at 10 microns. More consistent with the production line
The screen printing line width is gradually gradient from 25
25 line width
23 line width
21 line width
20 line width
18 line width
When the line width is wider, the printability is significantly improved, but the efficiency loss is greater and the wet weight is higher. When the line width is reduced to 18 microns, a large number of broken gates appear, and there is no advantage in efficiency. The final line width is determined at 20 microns.
After the parameters of the screen printing plate are determined, the efficiency of the finished screen printing plate will be increased by about 0.1%.
New diffusion process improves efficiency
Develop new processes through extensive experiments
oxygen flow gradient
anterior homologous gradient
Temperature gradient
Post-oxidation time and temperature gradient
Through combined experiments, it was determined to reduce the oxygen flow, fine-tune the front source, and make a high surface concentration shallow junction process, that is, the 0411 process
Different square resistance gradient experiment
Diffusion resistance gradient experiment
160Ω/□
170Ω/□
180Ω/□
Through multiple resistance switching experiments, it was determined that the 170 square resistance is relatively balanced in terms of efficiency and yield. When paired with the 0411 process, the efficiency can be improved by 0.05%.
SE square resistance reduction experiment
80Ω/□
90Ω/□
100Ω/□
The square resistance is reduced from 90Ω/□ and matched to 100Ω/□, and the efficiency is improved by 0.02%.
Etched high back polish
Debugging formulas with different acid ratios and comparing reflectivity differences
Rich hydrofluoric acid system
Determine the ratio of hydrofluoric acid to nitric acid to be 2:1
Rich nitric acid system
Determine the ratio of nitric acid to hydrofluoric acid to be 3:1
Track battery efficiency in two systems
The tracking results show that the hydrofluoric acid-rich system process has greater advantages, and the efficiency is 0.07 higher than the production line, rising from 22.60% to 22.68% (JA Solar products) with no abnormal appearance. The nitric acid-rich system process has poor process stability, and the appearance is difficult to satisfy customers. Require
Ultra-high back-throwing process reserve
During the process of debugging the formula, we experimented with a process with a backside reflectivity of up to 44%. Due to the large weight loss, it has a greater impact on the debris and rework yield, and is used as a process reserve.
Through extensive experiments, the etching formula was determined and the efficiency increased by about 0.07%.